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MAX1653ESE 参数 Datasheet PDF下载

MAX1653ESE图片预览
型号: MAX1653ESE
PDF下载: 下载PDF文件 查看货源
内容描述: 高效率, PWM ,降压型DC- DC控制器,16引脚QSOP [High-Efficiency, PWM, Step-Down DC-DC Controllers in 16-Pin QSOP]
分类和应用: 控制器
文件页数/大小: 28 页 / 266 K
品牌: MAXIM [ MAXIM INTEGRATED PRODUCTS ]
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Hig h -Effic ie n c y, P WM, S t e p -Do w n  
DC-DC Co n t ro lle rs in 1 6 -P in QS OP  
2–MAX165  
Bo o s t -S u p p ly Dio d e D2  
_____________Lo w -Vo lt a g e Op e ra t io n  
A 10mA to 100mA Schottky diode or signal diode such  
as a 1N4148 works well for D2 in most applications. If  
the input voltage can go below 6V, use a Schottky  
diode for slightly improved efficiency and dropout char-  
a c te ris tic s . Dont us e la rg e p owe r d iod e s s uc h a s  
1N5817 or 1N4001, since high junction capacitance  
can cause VL to be pumped up to excessive voltages.  
Low input voltages and low input-output differential volt-  
ages each require some extra care in the design. Low  
absolute input voltages can cause the VL linear regula-  
tor to enter dropout, and eventually shut itself off. Low  
input voltages relative to the output (low V -V  
differ-  
IN OUT  
ential) can cause bad load regulation in multi-output fly-  
back applications. See Transformer Design section.  
Finally, low V -V  
output voltage to sag when the load current changes  
abruptly. The amplitude of the sag is a function of induc-  
tor value and maximum duty factor (D  
Characteristics parameter, 98% guaranteed over tem-  
perature at f = 150kHz) as follows:  
differentials can also cause the  
IN OUT  
Re c t ifie r Dio d e D3  
(Tra n s fo rm e r S e c o n d a ry Dio d e )  
The secondary diode in coupled-inductor applications  
must withstand high flyback voltages greater than 60V,  
whic h us ua lly rule s out mos t Sc hottky re c tifie rs .  
Common silicon rectifiers such as the 1N4001 are also  
prohibited, as they are far too slow. This often makes  
fast silicon rectifiers such as the MURS120 the only  
choice. The flyback voltage across the rectifier is relat-  
an Electrical  
MAX  
2
(I  
STEP  
) x L  
V
SAG  
= ———————————————  
2 x C  
x (V  
x D  
- V  
)
OUT  
IN(MIN)  
MAX  
OUT  
ed to the V -V  
former turns ratio:  
difference according to the trans-  
IN OUT  
The cure for low-voltage sag is to increase the value of  
the output capacitor. For example, at V = 5.5V, V  
IN  
OUT  
V
= V  
+ (V - V  
) x N  
OUT  
FLYBACK  
SEC  
IN  
= 5V, L = 10µH, f = 150kHz, a total capacitance of  
660µF will prevent excessive sag. Note that only the  
capacitance requirement is increased and the ESR  
re q uire me nts d ont c ha ng e . The re fore , the a d d e d  
c a p a c ita nc e c a n b e s up p lie d b y a low-c os t b ulk  
capacitor in parallel with the normal low-ESR capacitor.  
Table 4 summarizes low-voltage operational issues.  
where: N is the transformer turns ratio SEC/PRI  
V
V
OUT  
is the maximum secondary DC output voltage  
is the primary (main) output voltage  
SEC  
Subtract the main output voltage (V  
) from V  
OUT FLYBACK  
in this equation if the secondary winding is returned to  
and not to ground. The diode reverse breakdown  
V
OUT  
rating must also accommodate any ringing due to leak-  
age inductance. D3s current rating should be at least  
twice the DC load current on the secondary output.  
Table 4. Low-Voltage Troubleshooting  
SOLUTION  
SYMPTOM  
CONDITION  
ROOT CAUSE  
Increase bulk output capacitance per  
formula above. Reduce inductor value.  
Sag or droop in V  
under step load change  
Low V -V  
<1V  
differential, Limited inductor-current slew  
rate per cycle.  
OUT  
IN OUT  
Dropout voltage is too  
Reduce f to 150kHz. Reduce MOSFET  
on-resistance and coil DCR.  
Low V -V  
<0.5V  
differential, Maximum duty-cycle limits  
exceeded.  
IN OUT  
high (V  
follows V as  
IN  
OUT  
V
IN  
decreases)  
Increase the minimum input voltage or  
ignore.  
Unstablejitters between Low V -V  
differential, Normal function of internal low-  
dropout circuitry.  
IN OUT  
two distinct duty factors  
<0.5V  
Not enough duty cycle left to  
differential, initiate forward-mode operation.  
Reduce f to 150kHz. Reduce secondary  
impedancesuse Schottky if possible.  
Stack secondary winding on main output.  
Secondary output wont  
support a load  
Low V -V  
IN OUT  
V
< 1.3 x V  
(main)  
Small AC current in primary cant  
store energy for flyback operation.  
IN  
OUT  
Use a small 20mA Schottky diode for  
boost diode D2. Supply VL from an  
external source.  
VL linear regulator is going into  
dropout and isnt providing  
good gate-drive levels.  
High supply current,  
poor efficiency  
Low input voltage, <5V  
Low input voltage, <4.5V  
Wont start under load or  
quits before battery is  
completely dead  
Supply VL from an external source other  
VL output is so low that it hits the  
VL UVLO threshold at 4.2V max.  
than V , such as the system 5V supply.  
BATT  
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