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LTC1624CS8 参数 Datasheet PDF下载

LTC1624CS8图片预览
型号: LTC1624CS8
PDF下载: 下载PDF文件 查看货源
内容描述: 高英法fi效率的SO-8 N沟道开关稳压器控制器 [High Efficiency SO-8 N-Channel Switching Regulator Controller]
分类和应用: 稳压器开关控制器
文件页数/大小: 28 页 / 493 K
品牌: Linear [ Linear ]
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LTC1624  
U
W U U  
APPLICATIONS INFORMATION  
with COUT, causing a rapid drop in VOUT. No regulator can  
deliver enough current to prevent this problem if the load  
switch resistance is low and it is driven quickly. The only  
solution is to limit the rise time of the switch drive so that  
the load rise time is limited to approximately (25 • CLOAD).  
Thus a 10µF capacitor would require a 250µs rise time,  
limiting the charging current to about 200mA.  
36V, most applications will be limited to 30V by the  
MOSFET BVDSS  
.
Modifying Burst Mode Operation  
The LTC1624 automatically enters Burst Mode operation  
at low output currents to boost efficiency. The point when  
continuous mode operation changes to Burst Mode op-  
eration scales as a function of maximum output current.  
The output current when Burst Mode operation com-  
mences is approximately 8mV/RSENSE (8% of maximum  
output current).  
Automotive Considerations: Plugging into the  
Cigarette Lighter  
As battery-powered devices go mobile there is a natural  
interest in plugging into the cigarette lighter in order to  
conserveorevenrechargebatterypacksduringoperation.  
But before you connect, be advised: you are plugging into  
the supply from hell. The main battery line in an automo-  
bileisthesourceofanumberofnastypotentialtransients,  
including load dump, reverse battery and double battery.  
WiththeadditionalcircuitryshowninFigure5theLTC1624  
can be forced to stay in continuous mode longer at low  
output currents. Since the LTC1624 is not a fully synchro-  
nous architecture, it will eventually start to skip cycles as  
the load current drops low enough. The point when the  
minimum on-time (450ns) is reached determines the load  
current when cycle skipping begins at approximately 1%  
of maximum output current. Using the circuit in Figure 5  
the LTC1624 will begin to skip cycles but stays in regula-  
Load dump is the result of a loose battery cable. When the  
cablebreaksconnection,thefieldcollapseinthealternator  
can cause a positive spike as high as 60V which takes  
several hundred milliseconds to decay. Reverse battery is  
just what it says, while double battery is a consequence of  
tow-truck operators finding that a 24V jump start cranks  
cold engines faster than 12V.  
tion when IOUT is less than IOUT(MIN)  
:
2
)
t
f
ON MIN  
(
V + V  
IN  
D
I
=
V V  
IN OUT  
(
)
OUT MIN  
(
)
2L  
V
+ V  
OUT D  
ThenetworkshowninFigure4isthemoststraightforward  
approach to protect a DC/DC converter from the ravages  
of an automotive battery line. The series diode prevents  
current from flowing during reverse battery, while the  
transient suppressor clamps the input voltage during load  
dump. Note that the transient suppressor should not  
conduct during double battery operation, but must still  
clamptheinputvoltagebelowbreakdownoftheconverter.  
Although the LTC1624 has a maximum input voltage of  
where tON(MIN) = 450ns, f = 200kHz.  
The transistor Q1 in the circuit of Figure 5 operates as a  
current source developing an 18mV offset across the  
V
IN  
+
C
R
SENSE  
IN  
1000pF  
100Ω  
18mV  
V
IN  
SENSE  
+
12V  
50A I  
PK  
Q1  
2N2222  
RATING  
LTC1624  
V
IN  
TG  
LTC1624  
R*  
TRANSIENT VOLTAGE  
SUPPRESSOR  
L1  
V
SW  
– 0.7V)  
OUT  
GENERAL INSTRUMENT  
1.5KA24A  
+
D1  
MBRS340T3  
C
OUT  
(V  
OUT  
180µA  
*R =  
1624 F04  
1624 F05  
Figure 4. Plugging into the Cigarette Lighter  
Figure 5. Modifying Burst Mode Operation  
12