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LP2951CNG 参数 Datasheet PDF下载

LP2951CNG图片预览
型号: LP2951CNG
PDF下载: 下载PDF文件 查看货源
内容描述: [100 mA, Low Power Low Dropout Voltage Regulator]
分类和应用: 光电二极管输出元件调节器
文件页数/大小: 22 页 / 188 K
品牌: ONSEMI [ ONSEMI ]
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LP2950, LP2951, NCV2951  
V
in  
for reducing noise on the 3 lead LP2950. However,  
increasing the capacitor from 1.0 mF to 220 mF only  
decreases the noise from 430 mV to 160 mVrms for a 100 kHz  
bandwidth at the 5.0 V output.  
Noise can be reduced fourfold by a bypass capacitor  
across R1, since it reduces the high frequency gain from 4  
to unity. Pick  
100 k  
5
8
V
in  
1
Error  
Output  
V
out  
Error  
V
out  
1.23 to 30 V  
2
NC  
NC  
SNS  
1
C
[
R1  
Shutdown  
Input  
3
Bypass  
6
2pR1 x 200 Hz  
0.01 mF  
SD  
V T  
O
3.3 mF  
or about 0.01 mF. When doing this, the output capacitor must  
be increased to 3.3 mF to maintain stability. These changes  
reduce the output noise from 430 mV to 126 mVrms for a  
100 kHz bandwidth at 5.0 V output. With bypass capacitor  
added, noise no longer scales with output voltage so that  
improvements are more dramatic at higher output voltages.  
GND FB  
4
7
R
2
Figure 19. Adjustable Regulator  
Unregulated  
Input  
MTB23P06E  
The complete equation for the output voltage is:  
1.0 mF  
10 k  
0.01 mF  
(
)
V
+ V  
1 ) R1ńR2 ) I  
R1  
out  
ref  
FB  
V
out  
5.0 V 1.0%  
0 to 1.0 A  
where V is the nominal 1.235 V reference voltage and I  
ref  
FB  
8
is the feedback pin bias current, nominally 20 nA. The  
minimum recommended load current of 1.0 mA forces an  
upper limit of 1.2 MW on the value of R2, if the regulator  
V
in  
1
2
5
3
Error  
Output  
V
Error  
out  
SNS  
LP2951CN  
must work with no load. I will produce a 2% typical error  
FB  
in V which may be eliminated at room temperature by  
out  
6
Shutdown  
Input  
SD  
V
O
T
220 mF  
adjusting R1. For better accuracy, choosing R2 = 100 k  
reduces this error to 0.17% while increasing the resistor  
program current to 12 mA. Since the LP2951 typically draws  
75 mA at no load with Pin 2 open circuited, the extra 12 mA  
of current drawn is often a worthwhile tradeoff for  
eliminating the need to set output voltage in test.  
GND FB  
4
7
0.002 mF  
1.0 M  
2.0 k  
Output Noise  
In many applications it is desirable to reduce the noise  
present at the output. Reducing the regulator bandwidth by  
increasing the size of the output capacitor is the only method  
Figure 20. 1.0 A Regulator with 1.2 V Dropout  
www.onsemi.com  
10