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LM2576-ADJ 参数 Datasheet PDF下载

LM2576-ADJ图片预览
型号: LM2576-ADJ
PDF下载: 下载PDF文件 查看货源
内容描述: 轻松切换3.0A降压稳压器 [Easy Switcher 3.0A Step-Down Voltage Regulator]
分类和应用: 稳压器
文件页数/大小: 28 页 / 288 K
品牌: MOTOROLA [ MOTOROLA ]
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LM2576  
Do Not Operate an Inductor Beyond its  
Maximum Rated Current  
Figure 24. Discontinuous Mode Switching Current  
Waveforms  
Exceeding an inductor’s maximum current rating may  
cause the inductor to overheat because of the copper wire  
losses, or the core may saturate. Core saturation occurs  
when the flux density is too high and consequently the cross  
sectional area of the core can no longer support additional  
lines of magnetic flux.  
This causes the permeability of the core to drop, the  
inductance value decreases rapidly and the inductor begins  
to look mainly resistive. It has only the DC resistance of the  
winding. This can cause the switch current to rise very rapidly  
and force the LM2576 internal switch into cycle–by–cycle  
current limit, thus reducing the DC output load current. This  
can also result in overheating of the inductor and/or the  
LM2576. Different inductor types have different saturation  
characteristics, and this should be kept in mind when  
selecting an inductor.  
0.4 A  
Inductor  
Current  
Waveform  
0 A  
0.4 A  
Power  
Switch  
Current  
Waveform  
0 A  
HORIZONTAL TIME BASE: 5.0 µs/DIV  
GENERAL RECOMMENDATIONS  
to smooth the output by means of an additional LC filter (20 µH,  
100 µF), that can be added to the output (see Figure 34) to  
further reduce the amount of output ripple and transients.  
With such a filter it is possible to reduce the output ripple  
voltage transients 10 times or more. Figure 25 shows the  
difference between filtered and unfiltered output waveforms  
of the regulator shown in Figure 34.  
The lower waveform is from the normal unfiltered output of  
the converter, while the upper waveform shows the output  
ripple voltage filtered by an additional LC filter.  
Output Voltage Ripple and Transients  
Source of the Output Ripple  
Since the LM2576 is a switch mode power supply  
regulator, its output voltage, if left unfiltered, will contain a  
sawtooth ripple voltage at the switching frequency. The  
output ripple voltage value ranges from 0.5% to 3% of the  
output voltage. It is caused mainly by the inductor sawtooth  
ripple current multiplied by the ESR of the output capacitor.  
Short Voltage Spikes and How to Reduce Them  
The regulator output voltage may also contain short  
voltage spikes at the peaks of the sawtooth waveform (see  
Figure 25). These voltage spikes are present because of the  
fast switching action of the output switch, and the parasitic  
inductance of the output filter capacitor. There are some  
other important factors such as wiring inductance, stray  
capacitance, as well as the scope probe used to evaluate  
these transients, all these contribute to the amplitude of these  
spikes. To minimize these voltage spikes, low inductance  
capacitors should be used, and their lead lengths must be  
kept short. The importance of quality printed circuit board  
layout design should also be highlighted.  
Heatsinking and Thermal Considerations  
The Through–Hole Package TO–220  
The LM2576 is available in two packages, a 5–pin  
TO–220(T, TV) and a 5–pin surface mount D PAK(D2T).  
Although the TO–220(T) package needs a heatsink under  
most conditions, there are some applications that require no  
heatsink to keep the LM2576 junction temperature within the  
allowed operating range. Higher ambient temperatures  
require some heat sinking, either to the printed circuit (PC)  
board or an external heatsink.  
2
2
The Surface Mount Package D PAK and its Heatsinking  
2
The other type of package, the surface mount D PAK, is  
designed to be soldered to the copper on the PC board. The  
copper and the board are the heatsink for this package and  
the other heat producing components, such as the catch  
diode and inductor. The PC board copper area that the  
Figure 25. Output Ripple Voltage Waveforms  
Voltage spikes  
caused by  
switching action  
of the output  
switch and the  
parasitic  
Filtered  
Output  
Voltage  
2
package is soldered to should be at least 0.4 in (or  
2
260 mm ) and ideally should have 2 or more square inches  
inductance of the  
2
output capacitor  
(1300 mm ) of 0.0028 inch copper. Additional increases of  
2
2
copper area beyond approximately 6.0 in (4000 mm ) will  
not improve heat dissipation significantly. If further thermal  
improvements are needed, double sided or multilayer PC  
boards with large copper areas should be considered. In  
order to achieve the best thermal performance, it is highly  
recommended to use wide copper traces as well as large  
areas of copper in the printed circuit board layout. The only  
exception to this is the OUTPUT (switch) pin, which should  
not have large areas of copper (see page 8 ’PCB Layout  
Guideline’).  
Unfiltered  
Output  
Voltage  
HORIZONTAL TIME BASE: 5.0 µs/DIV  
Minimizing the Output Ripple  
In order to minimize the output ripple voltage it is possible  
to enlarge the inductance value of the inductor L1 and/or to  
use a larger value output capacitor. There is also another way  
17  
MOTOROLA ANALOG IC DEVICE DATA  
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