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LT1175CS8#PBF 参数 Datasheet PDF下载

LT1175CS8#PBF图片预览
型号: LT1175CS8#PBF
PDF下载: 下载PDF文件 查看货源
内容描述: [LT1175 - 500mA Negative Low Dropout Micropower Regulator; Package: SO; Pins: 8; Temperature Range: 0°C to 70°C]
分类和应用: 稳压器调节器光电二极管输出元件
文件页数/大小: 16 页 / 291 K
品牌: LINER [ LINEAR TECHNOLOGY ]
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LT1175
APPLICATIONS INFORMATION
Note to Reader:
To avoid confusion when working with
negative voltages (is – 6V more or less than – 5V?), I have
decided to treat the LT1175 as if it were a positive
regulator and express all voltages as positive values, both
in text and in formulas. If you do the same and simply add
a negative sign to the eventual answer, confusion should
be avoided. Please don’t give me a hard time about
“preciseness” or “correctness.” I have to field phone calls
from around the world and this is my way of dealing with
a multitude of conventions. Thanks for your patience.
Setting Output Voltage
The LT1175 adjustable version has a feedback sense
voltage of 3.8V with a bias current of approximately 75nA
flowing out of the SENSE pin. To avoid output voltage
errors caused by this current, the output divider string
(see Figure 1) should draw about 25µA. Table 1 shows
suggested resistor values for a range of output voltages.
The second part of the table shows resistor values which
draw only 10µA of current. Output voltage error caused by
bias current with the lower valued resistors is about 0.4%
maximum and with the higher values, about 1% maxi-
mum. A formula is also shown for calculating the resistors
for any output voltage.
Table 1
OUTPUT
VOLTAGE
5V
6V
8V
10V
12V
15V
R1
I
DIV
= 25
µ
A
150k
150k
150k
150k
150k
150k
R2
R1
NEAREST 1% I
DIV
= 10
µ
A
47.5k
86.6k
165k
243k
324k
442k
383k
383k
383k
383k
383k
383k
R2
NEAREST 1%
121k
221k
422k
619k
825k
1.13M
R1
=
R2
=
3.8V
I
DIV
R1 V
OUT
3.8V
OUT
) (
Simple formula
)
3.8V
R1
(
V
3.8V
)
Taking SENSE pin bias
R2
=
3.8V
+
R1
(
I
)
current into account
FB
(
I
DIV
=
Desired divider current
6
U
W
U
U
The LT1175-5 is a fixed 5V design with the SENSE pin
acting as a Kelvin connection to the output. Normally the
SENSE pin and the OUTPUT pin are connected directly
together, either close to the regulator or at the remote load
point.
SHUTDOWN
LOGIC
> 2V OR < –2V TO
TURN REGULATOR ON
+
C
IN
+
SHDN
INPUT
I
LIM2
I
LIM4
LT1175
OUT
GND
SENSE
R1
383k
1%
R2
825k
1%
C
OUT
0.1µF
V
OUT
–12V
1175 F01
Figure 1. Typical LT1175 Adjustable Connection
Setting Current Limit
The LT1175 uses two I
LIM
pins to set current limit (typical)
at 200mA, 400mA, 600mA or 800mA. The corresponding
minimum guaranteed currents are 130mA, 260mA, 390mA
and 520mA. This allows the user to select a current limit
tailored to his specific application and prevents the situa-
tion where short-circuit current is many times higher than
full-load current. Problems with input supply overload or
excessive power dissipation in a faulted load are pre-
vented. Power limiting in the form of foldback current limit
is built in and reduces current limit as a function of input-
to-output voltage differential for differentials exceeding
14V. See the graph in Typical Performance Characteristics.
The LT1175 is guaranteed to be blowout-proof regardless
of current limit setting. The power limiting combined with
thermal shutdown protects the device from destructive
junction temperatures under all load conditions.
Shutdown
In shutdown, the LT1175 draws only about 10µA. Special
circuitry is used to minimize increases in shutdown cur-
rent at high temperatures, but a slight increase is seen
above 125°C. One option
not taken
was to actively pull
down on the output during shutdown. This means that the
output will fall slowly after shutdown is initiated, at a rate
determined by load current plus the 12µA internal load,
and the size of the output capacitor. Active pull-down is
1175fd