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AAT1140IGV-1.8-T1 参数 Datasheet PDF下载

AAT1140IGV-1.8-T1图片预览
型号: AAT1140IGV-1.8-T1
PDF下载: 下载PDF文件 查看货源
内容描述: 快速瞬态600mA降压转换器 [Fast Transient 600mA Step-Down Converter]
分类和应用: 转换器
文件页数/大小: 19 页 / 1021 K
品牌: ANALOGICTECH [ ADVANCED ANALOGIC TECHNOLOGIES ]
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PRODUCT DATASHEET  
AAT1140  
SwitchRegTM  
FastTransient 600mA Step-Down Converter  
Efficiency  
Layout  
Besides the AAT1140 device losses including switching  
losses, conduction losses, and quiescent current losses,  
the inductor copper loss also affects the efficiency of the  
buck converter. To the buck converter, the average cur-  
rent of the inductor is equal to output current IO. So the  
loss in the inductor is:  
The suggested 2-layer PCB layout for the AAT1140 is  
shown in Figures 2, 3 and 4. The following guide lines  
should be used to help ensure a proper layout.  
1. The power traces (GND, LX, VIN) should be kept  
short, direct, and wide to allow large current flow.  
Place sufficient multiple-layer pads when needed to  
change the trace layer.  
2. The input capacitor (C1) should connect as closely  
as possible to IN and GND.  
PLOSS_L = IO2 · RL  
3. The output capacitor C2 and L1 should be connected  
as closely as possible. The connection of L1 to the LX  
pin should be as short as possible and there should  
not be any signal lines under the inductor.  
4. The feedback trace or OUT pin should be separate  
from any power trace and connect as closely as pos-  
sible to the load point. Sensing along a high-current  
load trace will degrade DC load regulation. If exter-  
nal feedback resistors are used, they should be  
placed as closely as possible to the OUT pin to min-  
imize the length of the high impedance feedback  
trace.  
Table 4 shows some recommended inductors. A larger  
size inductor usually has smaller DCR. As a example: if  
selecting CDRH2D14 4.7μH for 1.8V output, the PLoss_L is  
48.6mW when output current is 600mA, so the inductor  
loses 4.5% power; if selecting CDRH3D23 4.7μH, the  
PLoss_L should be 19.8mW, and the inductor losing power  
ratio is only 1.8%. The inductor size and the buck con-  
verter efficiency is always a trade-off in the real applica-  
tion.  
5. The resistance of the trace from the load return to  
GND should be kept to a minimum. This will help to  
minimize any error in DC regulation due to differ-  
ences in the potential of the internal signal ground  
and the power ground.  
w w w . a n a l o g i c t e c h . c o m  
1140.2007.12.1.1  
15  
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